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76 gmc swb from he--!!
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so its like this...y'all have heard me go on about this truck and kept asking for some pics so here are a few basic ones too start...remember i said it aint much to look at yet...upon purchasing my truck for 400$ i thought i had gotten a deal.. i only had time for a quick look before saving it from salvage yard the wrecker was allready on the way...after getting it home and inder the microscope i found "cancer in the floors, more additional wiring than i thought was possible.. someone had removed the original inline 6 to install a smallblock.since they didnt know you could/had to move the motor mounts they just unbolted the plate from passenger side of block and let it lay on its side...thinking they were slick they added a chain to hold it down but put it on same side as the mount that was bolted in...looks like the hole in the tunnel for 3spd shifter was cut with a sledgehammer and a crowbar..when i picked up the truck to bring it home the 3spd trans was in the bed and i found an auto and torque converter in bushes so i grabbed it too..it was a 200-4r...after the major inspection and gutting of the interior and almost all of the "aftermarket wiring" i put a battery in and took a gamble and turned the key and pushed the button..the motor turned over and with a little priming started..i let it run for about a minute and turned it off only to hear dripping water...it was coming from every where..left side, right side, back, front, every where every freeze plug was completely rusted out...so i pulled the motor installed brass plugs, corrected the mounting with new mounts in correct location, gave it a new oil pan gasket since i had it out beside there was a dent in oil pan i had to fix...gave about 2 seconds to the thought of stripping and painting the motor but nah not yet...put it back into the truck with the 200-4r trans, called up bowtie overdrive got all the wiring and went to fill it up and see if it would move nope DENIED...apparently someone had jammed the pump..so once again back on the net for parts..put a 13 vane upgrade kit in and put trans back in and yeeha it moved...in the process of putting all new brakes and soon all poly in suspension got to make it stick to curvy country roads..oh yeah and the multi sized, 57 welds, blown glasspack havin exhaust, sounded like crap so i picked up a complete 2010 nissan titan exhaust and with 3 cuts grafted it in now it sounds much much better...now i got 1 bucket seat from some kind of car no floor no dash no tunes but it will take me to the beer store...lol more upgrade to come soon along with cosmetic work and lots of new pics i hope
Attachment 778437 ive been doing some testing with rattle can first to see what colors i want...lol Attachment 778438 Attachment 778440 heres my 72 datsun 240z Attachment 778441 and cant leave out the jeep...just removed exo and emptied out the carriers to get bigger gears and moved the front axle forward 4 more inches for better approach Attachment 778442 |
Re: 76 gmc swb from he--!!
Not bad for $400. You just saved a square from the crusher. Your my hero!
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Re: 76 gmc swb from he--!!
5 Attachment(s)
ok heres some more pics from interior and engine bay
Attachment 778609 "flintstonin" Attachment 778610 Attachment 778611 crappy tired old ugly 350...seems to run pretty good tho Attachment 778612 still a little "aftermarket wiring to clean up" Attachment 778613 once i have everything mechanical and electrical is working ill tear it all down for clean up and cosmetics.... |
Re: 76 gmc swb from he--!!
Those floors remind me of my truck and the Six Million Dollar Man tv show from the '70s:
" We can rebuild him..." Great progress so far! Keep it up!! |
Re: 76 gmc swb from he--!!
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Re: 76 gmc swb from he--!!
is that a 850 i spot behind the jeep thing
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Re: 76 gmc swb from he--!!
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yes...its a 93 model...wish i had known about the parts issues with 93's...3 years ago i hydralocked the motor, and bent a rod...so i tore it down checked everything, cleaned up the pistons and rings using acetone and trans fluid mixture...threw a set of rod bearings and 1 new rod at it, literally reused everything else except gaskets..and shes still rocketing down the road |
Re: 76 gmc swb from he--!!
well finally got a working radiator...fabbed in one from a 86 k-5...original radiator had 29 rows and 2 cores where as the new one has 50 rows with 2 cores...now i need front rotors and ill finally be able to drive it and dial in my tv cable for my overdrive...on a different note i finally brought my 78 fs bronco back home from tn....the c-6 has given up the ghost and wont back up n e more....gonna do some clean up and metal repair on the floors and will have more pics n a couple days ......cheers till then
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Re: 76 gmc swb from he--!!
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awwwwwwwwwwwwwwv yeahhhhh more pics............ my other trucks....however the jeep is moving to a new shell
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Re: 76 gmc swb from he--!!
well took the first maiden voyage away from home in the gmc today...went to the scrapyard...got enough spare change to get more parts...yay
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Re: 76 gmc swb from he--!!
well finally got the front side of the core support all cleaned up and painted, i really wish one of my headlight bezels didnt have a small crack but hey whatever...the nasty grill cleaned up ok but will get an aftermarket grill at some point...oh yeah n finaly got timing close to correct...cant really tell for surre as untill teardown i wont know what if any type of cam i have...doesnt seem to idle like it has one so im guessing its close or is stock.....will post some pics in a bit
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