The 1947 - Present Chevrolet & GMC Truck Message Board Network







Register or Log In To remove these advertisements.

Go Back   The 1947 - Present Chevrolet & GMC Truck Message Board Network > General Truck Forums > Engine & Drivetrain

Web 67-72chevytrucks.com


Reply
 
Thread Tools Display Modes
Old 08-18-2015, 10:18 AM   #1
KyleSeal
Senior Member
 
KyleSeal's Avatar
 
Join Date: Mar 2014
Location: Toano, VA
Posts: 893
Removing Saginaw from 350

So I did my first engine removal the other night. Now, onto disassembly.

Heres my problem: Removed all the bolts to the bellhousing, tried to pull the trans (with bellhousing) and it came out a little, maybe a half an inch, but no more.

My question(s): is this normal? If so, how can I remove it further? My dad said he thinks its hanging up on the input shaft. Is there anything I need to further disassemble?

Any pictures would help greatly.

Info: SB350, Saginaw 3 speed.

Thanks.
__________________
"Sometimes I do serve as a good bad example. Glad to be of service."

My Build Thread (1967 C10, lowered, EFI, daily truck): http://67-72chevytrucks.com/vboard/s...d.php?t=830809
KyleSeal is offline   Reply With Quote
Old 08-18-2015, 10:39 AM   #2
crazy longhorn
Fabricate till you "puke"
 
Join Date: Jun 2002
Location: Ill
Posts: 9,402
Re: Removing Saginaw from 350

Do you have the tin dust cover off the bottom, & the starter removed? longhorn
__________________
69 longhorn,4" chop,3/5 drop, 1/2 ton suspension/disc brakes,1 1/2" body drop,steel tilt clip, 5.3/Edelbrock rpm intake/600 carb, Hooker streetrod shorties,2 1/2" exhaust/ H pipe/50's Flows , 6 spd Richmond trans,12 bolt/ 3.40 gears....
crazy longhorn is offline   Reply With Quote
Old 08-18-2015, 10:53 AM   #3
KyleSeal
Senior Member
 
KyleSeal's Avatar
 
Join Date: Mar 2014
Location: Toano, VA
Posts: 893
Re: Removing Saginaw from 350

Yes, I do.
__________________
"Sometimes I do serve as a good bad example. Glad to be of service."

My Build Thread (1967 C10, lowered, EFI, daily truck): http://67-72chevytrucks.com/vboard/s...d.php?t=830809
KyleSeal is offline   Reply With Quote
Old 08-18-2015, 11:00 AM   #4
mongocanfly
Post Whore

 
mongocanfly's Avatar
 
Join Date: May 2015
Location: Alabama
Posts: 14,673
Re: Removing Saginaw from 350

If you've cleared the engine dowel pins then most likely its the input shaft stuck in the clutch disc. Keep on prying......

Last edited by mongocanfly; 08-18-2015 at 11:11 AM.
mongocanfly is offline   Reply With Quote
Old 08-18-2015, 11:11 AM   #5
KyleSeal
Senior Member
 
KyleSeal's Avatar
 
Join Date: Mar 2014
Location: Toano, VA
Posts: 893
Re: Removing Saginaw from 350

So if I keep pulling it should come off? Will the resistance be the same or will it sort of pop off?
__________________
"Sometimes I do serve as a good bad example. Glad to be of service."

My Build Thread (1967 C10, lowered, EFI, daily truck): http://67-72chevytrucks.com/vboard/s...d.php?t=830809
KyleSeal is offline   Reply With Quote
Old 08-18-2015, 11:16 AM   #6
mongocanfly
Post Whore

 
mongocanfly's Avatar
 
Join Date: May 2015
Location: Alabama
Posts: 14,673
Re: Removing Saginaw from 350

It should come loose if you keep working on it..sometimes if there is wear on the shaft or clutch it can make it harder to come apart..if you have it in the floor the trans centerline still needs to be somewhat lined up with the engine centerline until it clears the clutch..if you pull it out part way and let the trans drop out of centerline it will cause it to bind up..try holding up on the tailshaft and pry at the same time..may take 2 people..

Last edited by mongocanfly; 08-18-2015 at 11:21 AM.
mongocanfly is offline   Reply With Quote
Old 08-18-2015, 01:02 PM   #7
KyleSeal
Senior Member
 
KyleSeal's Avatar
 
Join Date: Mar 2014
Location: Toano, VA
Posts: 893
Re: Removing Saginaw from 350

Just got it out a little bit ago, ironically I dropped the engine lift an inch and yanked and it popped out. Thanks for the help, I appreciate it. Hopefully this thread helps someone like me with the same problem.
__________________
"Sometimes I do serve as a good bad example. Glad to be of service."

My Build Thread (1967 C10, lowered, EFI, daily truck): http://67-72chevytrucks.com/vboard/s...d.php?t=830809
KyleSeal is offline   Reply With Quote
Reply

Bookmarks

Tags
1970, 3 speed, 350, chevrolet, saginaw

Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -4. The time now is 02:19 PM.


Powered by vBulletin® Version 3.8.11
Copyright ©2000 - 2024, vBulletin Solutions Inc.
Copyright 1997-2022 67-72chevytrucks.com