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06-29-2002, 11:26 AM | #1 |
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exhaust stud removal
anyone who has any good tips regarding removing frozen and busted off flush exhaust flange studs please post their info here
got one thats busted off flush that i gotta get out, worst case scenario is that I would have to drill out 3/8" and use nut and stud.... |
06-29-2002, 11:53 AM | #2 |
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Location: Victoria, BC, Canada
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The last resort is drilling, they just never seem to fit right after that. Unless you can drill it out at a near perfect right angle to the flange and tap it for a larger size stud. The steel they use for these things is extremely hard, went thru a couple drill bits (with numerous resharpenings in between) just on one hole.
Best bet is to drill part way w/ a smaller size bit than the hole. Then heat the hell out of it with a torch, squirt penetrating oil and use an "easy-out".
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06-29-2002, 12:12 PM | #3 |
70 Chevy 3/4t
Join Date: Sep 2000
Location: Kokomo,IN USA
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I had to do this to the exhaust manifold on my I6. Believe it or not I actually got one of them to screw out.(lots of PB, LOL) the other snapped when I tried to remove it.
First grind it off flush, find the center of the stud and centerpunch it. Then start with a small drill bit and go through it and slowly increase size of bit. Then get a easy out and hope the remaining metal comes out. If not, you can retap the hole.
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06-29-2002, 12:29 PM | #4 |
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Location: Saskatoon,SK,Canada
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Take it to somebody with a mig welder and put a nut over what is left of the stud. If the stud is flush carefully build up the stud with the mig until you have enough to weld to. Weld the nut on and the heat from that will likely have loosened the threads. Just turn it out with a wrench then. If that fails drill and easy out but use some heat to help loosen the threads.
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06-29-2002, 01:17 PM | #5 |
CCRider
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Location: Olive Branch,MS,USA
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I aways grind them flush, drill them out, then use helicoils. You don't have to drill it perfect because you are going to tap it out to a bigger size for the helicoil. After you install it it is back to the correct size and the threads are now stainless steel so no more problems. When you get new studs, get the kind that come with brass nuts.
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06-29-2002, 05:08 PM | #6 |
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Use a reversible drill and reverse cut bits for your drilling and it might spin it's self out, if not you'll have your hole for easy-outs. I did this once and when I moved up in bit size it spun it out.
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06-29-2002, 05:30 PM | #7 |
aka Crusher, Crushergmc
Join Date: Mar 2000
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If you use stainless helicoil, don't use stainless studs. Stainless +stainless + heat = gauling. Bad news.
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07-06-2002, 06:52 PM | #8 |
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thanks guys, well im gonna try drill and EZ out and heat and hope for best, only bad thing about heat is that heat changes properties of metals and makes them brittle, so,,,
but have no choice really,,, thanks |
07-06-2002, 08:52 PM | #9 |
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What I have done in the past is this:
Drill the stud to the size you need for an E-Z out. don't tap in the E-Z out yet Get your fire-wrench out and get the manifold red hot. Try not to focus the heat on the stud. Now you have to move fast. Tap in the E-Z out and back out the remains of the stud. Cool things down, clean the threads, and put in a new stud.
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09-05-2002, 03:32 AM | #10 |
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awesome, thats very good info for the memory bank, now lets move over to broken 3/8" bolt in exhaust manifold mounting bolt snapped off in the (same bolt) hole in the head ?
3/8" with 16 tps helicoil ? what size tap do you have to use for 3/8" coil anyways? thats my Q, i have two i need to fix... asap. who has done it ? thanks for anything |
09-05-2002, 08:38 AM | #11 |
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Unlike the manfold stud that bottoms out on its "neck" when you tighten it down, the broken bolt in the head should NOT be, unless someone used the wrong bolt. Get yourself a reverse cut drill bit or one of the combo drill/srew removers and it SHOULD spin right out... but you know how that is All of the stress is off the threads once the bolt breaks, but the stress remains on the stud after it breaks because the shoulder is still snug against the manifold face.
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09-05-2002, 02:31 PM | #12 |
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wow, good point there, thanks!@
wel the problem is that the bolts snapped off in the head due to severe corrosion, so the odds of them spinning right out are very very slim,.. they are frozen corrode welded to in the bolt holes bad, must be a big block engien problem, never had it happen on a SBC engine thanks |
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