08-03-2002, 06:58 PM | #1 | |
Bloo
Join Date: Feb 2001
Location: Barren County Kentucky
Posts: 6,283
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just back from Huck's
just got back from the cookout at Huck's, meet oldpaint, high724x4, longhornmail, peirce, of course huck, and jamie, i think his board name is jamie72? i got his real nam ebut not the board name. got the 400SB from andy, andy got his chrome glovebox door, we all got some really good food, and talked trucks out on the back porch. i took some pics of the trucks, and of course andy (cut up ) possed next to the GMC. he said he thought his cam bearings were going though so if hes not on untill late late tonight we know to go looking for him along the interstates. also got pics of some street rods rolling down the interstate, and one of peirce's 37? i think was the year, chevy.
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ASE Master Certified-GM Trained-Mechanic 1968 Chevy C30 157" WB Wrecker 1969 Chevy CST/10 SWB 1971 Chevy Custom/10 (first truck) 350, NV3500 5 speed 1971 Chevy K20 Custom Camper 4x4 350 TBI, SM465/NP205 1974 Chevy Custom Deluxe/10 1979 Chevy Custom Deluxe K10 farm truck beater 1989 Chevy K2500 Quote:
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08-03-2002, 09:48 PM | #2 |
Account Suspended
Join Date: Jan 2000
Location: Woodstock, IL
Posts: 7,020
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Sounded like it was a good ole' time.
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08-04-2002, 12:12 AM | #3 |
Registered User
Join Date: Feb 2002
Location: Crawfordsville, IN USA
Posts: 84
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I sure wanted to go, but the lack of funds kept me close to home. I bet it was a really good time. Maybe I'll make it next time, I'd really like to meet some of you guys(and gals).
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1986 Silverado CrewCab Dually 454 auto. |
08-04-2002, 12:23 AM | #4 |
its all about the +6 inches
Join Date: Jan 2001
Location: Hilliard Ohio
Posts: 2,690
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I just got back about 20 min ago...(11:30-ish eastern) Trip went awsome. Everything went pretty close to planned for me.
Even though I did get lost and wandered around the backwoods areas...bout 50 - 60 miles added, scared to hell that my cam bearings were going to leave me stranded...almost out of gas, (had 1 gallon left by the time I found a pump) no one could give me good directions, and only one of those little towns had a gas station that i saw. Scared sh!tless. I had to ask 5 ppl how to get there, got 5 differant stories...and no one had a map (not even the gas station????) So anyways, I finally got there, we all meet, had some awsome eats, .B.S. around, then we look at my truck.... It was makin a very loud metalic grinding/squeeling noise...I was able to hear it over my pipes (or lack thereof) and through the ear plugs, the faster I went, the louder it got. I did the screwdriver to the ear trick, and discovered the water pump, alt, and power steering was all good, no noise. IT was coming from the front of the motor, and my oil psi hasn't been to great lately. Safe asumption. It was also running 200 - 210 instead of 160 - 180. Then huck discovers the fan clutch is locked up. WTF??? It was only 2 years old!!!!He pulled one out of a scrap pile, and INSTALLS IT for me!!!! Awsome huh? When the old one hits the grass, we pick it up, and make it turn in the clutch...there's my noise. Phew. Well, not only did it go flawless after that, but those torque pluss intake gaskets...AWSOME! I finaly tuned it with MUCh less timing, (10BTDC instead of about 16-18) Not only is the power alot better....the MPG went up from 9 - 10 up to 13 - 14 at a higher rate of speed. I averaged 80 all the way home and got 14. Awsome huh? Huck, thanks for the get together, glad to meet everyone....I had a blast. Last edited by Longhorn Man; 08-04-2002 at 10:59 AM. |
08-04-2002, 11:10 AM | #5 |
its all about the +6 inches
Join Date: Jan 2001
Location: Hilliard Ohio
Posts: 2,690
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ttt
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