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Old 05-30-2006, 11:03 PM   #1
Gray Ghost
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Ordeal is over....at least this part anyway.

I sure hate PO's. They do the dumbest ****.

This one had replaced the timing chain recently. Unfortunately, he reused a bad balancer and a bad timing chain cover and RTV'd the holy hell outta the darn thing to cover up the leak. No wonder it was for sale when the middle man got it.

Here's what happened. I had just put new wires on it and was on the way to an appointment in Cedar Hill. Two wires weren't on good and came off making the truck run badly. It actually backfired a few times on me [it may still since it did that before I swapped wires]. I stopped to check under the hood and saw oil dripping rapidly onto the crossmember. Checked the oil and I was three quarts low [I had just filled it the day before].

Heard what I thought was ticking noises and shut her down. It was actually the big exhuast leak I have....header gasket is bad on the passenger side.
So I get towed home on Memorial Day.

I tore it down that evening and found all the bad stuff he had done, went and got the balancer and verything except the gasket kit for the timing cover. Realized this morning that the cover was worse than I tought, so then the hunt was on. Finally found one in Mesquite at Performance Auto...no one in Terrell had one for a 70.

The balancer and timing cover gasket went on like a dream...the two things I thought would give me trouble. I bought an installer for the balancer and it was easy as all get out to install. Thanks to veryone who had suggestions about how to install it.

So now it's back together, but it still has two quirks....it 'backfires' [sorta hard to explain but it acts like it is gonna die, then goes back to normal right away].

Anyway the other one is it has a lot of little tiny 'stumbles' as it accelerates...almost as if it is way out of tune. Course it could be fuel oriented.

I am now out of cash to fix anything else past the exhaust gaskets, so I hope it runs ok tomorrow and the rest of the week.

If anyone can help me figure out what it's doin' and how to fix it, let me know. It only does those two things after it warms up. The 'backfire' is the most larming of the two...kinda remotely reminds me of the Buffalo's dropping 500 rpms, but a little bit different.
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Old 05-31-2006, 08:01 AM   #2
Palf70Step
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Re: Ordeal is over....at least this part anyway.

Sounds like a carb or fuel issue. I'd look for junk in the fuel filter and quiet possibly a carb rebuild. Especially from your description of the POs mechanical abilities.
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Old 05-31-2006, 08:44 AM   #3
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Re: Ordeal is over....at least this part anyway.

Sounds like a problem I was having with my 93 truck. After it would heat up it would start to stumble like it wanted to turn off. It ended up being the distributor. If you remove the cap and look straight down on it where the magnet is that was cracked in 4 places. That caused it to only fire on 1 side. I ended up having to replace the distributor and all is well. here is a link to a post that was put up befor on this problem. http://67-72chevytrucks.com/vboard/s...d.php?t=163377
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Old 06-01-2006, 06:39 PM   #4
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Re: Ordeal is over....at least this part anyway.

Well I was right in suspect the distributor, the windings on the pickup coil literally fell out of the coil when we took it out today.

No more jumpy tach and no more cutting out when it warms up!!

We also changed out the rear main seals and the pan gasket and installed a new oil dipstick.

I feel like I got a new truck again!! Runs like a champ!!!
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Old 06-01-2006, 07:53 PM   #5
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Re: Ordeal is over....at least this part anyway.

Good to hear!!!
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Old 06-01-2006, 08:41 PM   #6
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Re: Ordeal is over....at least this part anyway.

Glad to hear ya got it fixed
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Old 06-02-2006, 09:06 AM   #7
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Re: Ordeal is over....at least this part anyway.

Quote:
Originally Posted by Buffalo Elk
Well I was right in suspect the distributor, the windings on the pickup coil literally fell out of the coil when we took it out today.

No more jumpy tach and no more cutting out when it warms up!!

We also changed out the rear main seals and the pan gasket and installed a new oil dipstick.

I feel like I got a new truck again!! Runs like a champ!!!
glad to hear you fixed it.
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Old 06-02-2006, 07:42 PM   #8
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Re: Ordeal is over....at least this part anyway.

I shoulda kept my mouth shut. Today the ignition switch went out....a quick trip to Poop Boyz and the new part was installed....what a hassle getting the old one out!!
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Old 06-02-2006, 08:59 PM   #9
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Re: Ordeal is over....at least this part anyway.

Sounds like your typical truck stuff.
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Old 06-02-2006, 11:40 PM   #10
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Re: Ordeal is over....at least this part anyway.

there always something to fix on these. seems like i get 1 thing fixed and find 5 more. good luck. chris.
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