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Old 01-27-2003, 02:10 PM   #1
texnician01
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carb troubles

I've got a 69 with a 292 that I just drove out of the shop the other day after a 3 year restoration. It has a single barrel holley model number 1940 on it. the carb works good but it is acting up at the moment. it has a dead spot off of idle witch is exactly where it runs when cruising so I get this bucking and surging thing going on. then if I start up a hill on the highway or interstate it does the same thing wants to cut out and buck. the more I push the pedal the worse it gets. I jetted the thing down just a little before I stopped driving it but don't remember it doing this. If I reach down and pull out the choke a little it almost goes away, but I can't run around with the choke pulled out all the time. I'm sure it's not ignition cause I have an ignitor and most of the rest of it is in good shape. any suggestions?

thanks

Nathan
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Old 01-27-2003, 02:21 PM   #2
70c10
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Have you checked the fuel filter?
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1970 C/10 Fleetside w/Ghost Flames
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Old 01-27-2003, 02:27 PM   #3
texnician01
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has a brand new filter on it.
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Old 01-27-2003, 02:32 PM   #4
70c10
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Does it have the original accelerator pump?
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1970 C/10 Fleetside w/Ghost Flames
Lowered 4.5" front and 4" rear (Raked)
355/350 Turbo w/shift kit
10" Redneck Performance Verter w/2500 stall
Hooker Super Comps part#2808-1
Performer RPM Air-Gap
12 Bolt w/3:73 gears- Eaton Posi
Comp Cams XE262 with 1.6 Crane Energizers, Road Demon 625 and Brodix IK 180 heads
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Old 01-27-2003, 02:35 PM   #5
texnician01
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had a rebuild kit put in it about 6 months before I stopped driving it.

nathan
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05 Harley Night Train
06 1200 Sportster (Wife's bike)
70 Honda CL350


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Old 01-27-2003, 02:40 PM   #6
SWINGSAX68
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Hmm....same problem I had......very similar...not as much bucking...but it wouldn't clear an incline for damn sure...check the vacuum advance and makesure to check the timeing as well. that may help...just from what I think is going on.
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Old 01-27-2003, 03:07 PM   #7
68chevy10
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i had a similar problem with my 350, it was the mechanical fuel pump, it was puting out to much presure, does it blow black smoke?
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Old 01-27-2003, 03:09 PM   #8
texnician01
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ya it does and it has a fairly new pump on it.
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06 1200 Sportster (Wife's bike)
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Old 01-27-2003, 03:14 PM   #9
68chevy10
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ya my pump was also brand new, check fuel presure, it should be about 7-9 psi if i'm not mistaken. mine was putting out 14-15 psi, i don't know why, i installed a regulator on it and the problem was cured
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Old 01-27-2003, 03:35 PM   #10
sneakysnake
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sounds like a restricted main jet, by being able to pull the choke and it smooth out,you richen the mixture,sitting up may have produced some crud
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