08-21-2018, 07:41 PM | #1 |
Registered User
Join Date: Jun 2018
Location: Sacramento, California
Posts: 52
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No Crank Situation.
Hello gang, I will try to make this short. Today I started the 68 GMC and the wire to the kick down switch smoked itself. The acc hot wire had a bit of cracked insulation and grounded itself and smoked all the way to the fuse block. I shut the truck off, investigated the damage and then tried to start the truck. The engine wouldn't crank. So I started testing circuts. From the firewall half of the fuse block it is all ok. I ran a hot wire to the starting circut, big fat purple wire, and the starter spins and with the key on, will start. I'm getting juice into the ign switch, and getting juice thru the fat purple wire from the ign switch. I haven't cut into the under dash harness yet, I lost all of my patience by then. It acts like a neutral safety switch is bad or mis adjusted when you try to turn the key. All else seems to be working as it should. What am I missing? Again, thank you in advance for your help. Respectfully, Mark
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08-21-2018, 08:45 PM | #2 |
Post Whore
Join Date: Feb 2016
Location: Portland Oregon
Posts: 11,350
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Re: No Crank Situation.
Having had my ignition switch go bad recently I know that the ACC post on the switch and the SOL post are next to each other and the ACC being shorted may have melted the switch and the SOL post is no longer able to conduct electricity properly. Look at the last posting in my WMB thread below for more info and some pictures of how my switch was damaged. Try measuring the voltage at the neutral safety switch with it plugged in then unplug it it from the switch and measure it again. (While in the start position) It may help you trouble shoot the problem.
Good luck.
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Thanks to Bob and Jeanie and everyone else at Superior Performance for all their great help. RIP Bob Parks. 1967 Burban (the WMB),1988 S10 Blazer (the Stink10 II),1969 GTO (the Goat), 1970 Javelin, 1952 F2 Ford OHC six 4X4, 29 Model A, 72 Firebird (the DBP Bird). 85 Alfa Romeo If it breaks I didn't want it in the first place The WMB repair thread http://67-72chevytrucks.com/vboard/s...d.php?t=698377 |
08-21-2018, 09:12 PM | #3 | |
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Join Date: Jun 2018
Location: Sacramento, California
Posts: 52
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Re: No Crank Situation.
Quote:
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08-24-2018, 09:57 AM | #4 | |
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Join Date: Jun 2018
Location: Sacramento, California
Posts: 52
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Quote:
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08-24-2018, 10:03 AM | #5 |
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Join Date: Jun 2018
Location: Fuquay-Varina, NC (Just outside of Raleigh)
Posts: 237
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Re: No Crank Situation.
If the sending unit was corroded, how was the tank? A new sock might get you by, but might want to think about replacing or cleaning the tank if it is corroded as well.
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1972 C-10 [Boppa's Truck] |
08-27-2018, 01:14 AM | #6 |
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Join Date: Jun 2018
Location: Sacramento, California
Posts: 52
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Re: No Crank Situation.
I shined a flashlight into the tank through the filler neck, and it appears that the corrosion is loose and very light. It has accumulated on about the top 6-10 inches of the tank, and at the bottom which I believe is from the crud washing off the sides of the tank. The interior of the tank is shiny otherwise. I'm debating on a 5 pound bag of gravel and some water in it anyhow since the truck has a new motor, and I have a brand new carb ready for installation. The sender is on order, and will not be here until the end of the week.
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08-27-2018, 01:16 AM | #7 |
Registered User
Join Date: Jun 2018
Location: Sacramento, California
Posts: 52
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Re: No Crank Situation.
Rut Row! I've hijacked my own thread.
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