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08-03-2022, 01:43 PM | #1 | |
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Join Date: Apr 2016
Location: Sacramento, CA
Posts: 11
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
I went through a similar problem with my 292, replaced many parts just as you during the process of elimination. All of the items helped, HEI, fuel pump, filter, carb rebuild, etc. but problem would return after awhile. Turned out the fuel tank had rust buildup that would come loose, plug a carb jet or eventually plug the fuel filter. Pulled the carb apart several times to just find more rust getting past filter. Cleaned it all out and ran great! Just my 2 cents.
Quote:
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1968 GMC 1500 LWB 350 V8/TH700R4 1970 CST-10 SWB 350 V8/3-Spd Saginaw 1967 C-10 |
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08-03-2022, 09:17 PM | #2 |
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Join Date: Jun 2017
Location: Painesville, OH
Posts: 180
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
RICHARDJ
One question or yours that I forgot to answer. The Intake/Exhaust gaskets were replaced last year. Still look good. No black soot around this area. |
08-03-2022, 09:21 PM | #3 |
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Join Date: Jun 2017
Location: Painesville, OH
Posts: 180
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
RICHARDJ
One question of yours I forgot to answer. The Intake/Exhaust gaskets were replaced last year. They still look good and there is no black soot around that area. Thanks. |
08-12-2022, 03:59 PM | #4 |
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Join Date: Jun 2017
Location: Painesville, OH
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
UPDATE:
Carburetor came back from the shop and everything checks out ok. I pulled the distributor and put new points and condensor in even though points looked good and condensor was a year old. New issue. I marked the distributor and motor so I could just drop it back in. I also took a picture of which way the rotor was pointing. When I try to reinstall, the distributor will only seat with the rotor pointing another direction. Why? Should it not go back in the way it was? The truck was not moved and or cranked while distributor was out. First pic is before I pulled it. Second pic is how it now seats... uuugh! Help! |
08-02-2022, 11:35 PM | #5 |
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Location: So Cal
Posts: 1,458
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
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* * * * * Confirmed vacuum advance arm is working -- vac adv should be connected to Ported Vacuum port with no advance @ idle with 0 in.hg. * Checked vacuum at carb -- Vacuum = ? in.hg. @ rpm, checked WHERE ? Port on manifold or does you carb have manifold vacuum port? * Confirmed points/dwell set properly -- With vacuum hose plugged, does dwell stay @31 when engine is revved, With engine @idle, use hand vacuum pump to operate vacuum advance through its full range. Watch timing on balancer with timing light. Again check that dwell stays @ the 31 * Confirmed RPMs -- What is the Idle rpm with choke off and engine warm New exhaust -- Did you check the Intake/Exhaust gasket against the head? Look for black soot on the block below the manifolds. NEW Exhaust? Did you get the LMC exhaust?
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'67 GMC 2500, 292, 4spd, AC |
08-03-2022, 09:10 AM | #6 | |
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Join Date: Jun 2017
Location: Painesville, OH
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
Quote:
I'm a do it yourself mechanic so please forgive me if my answers don't make sense or I'm not understanding something.. Vacuum advance is connected to port on carb in the picture I have attached. When disconnecting and checking with vacuum guage and engine at idle the guage read 0. When revving the engine the guage would read up to 20. I did not have a meter hooked up for RPMs when revving the engine. Idle for this motor with choke off and warmed up is 700rpm. I believe normally it would be 400rpm but according to the shop manual it should be 700rpm because mine has the A.I.R. smog pump. I have not checked your third suggestion. Will do that. I ended up getting the LMC exhaust. Ended up working out good. Thanks for everyone's help... Hope to get this figured out soon. |
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08-04-2022, 07:47 AM | #7 |
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Join Date: Jan 2019
Location: St Peters, MO
Posts: 440
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
Sounds similar to my issue last year: Truck had an occasional backfire or load up when driving. It progressively got worse to where it would start OK, but would die when put into gear. It would idle and rev OK, but ran badly under a load, or when stopping at a stoplight. I had to put it in neutral a few times to keep it from dying at intersections. Later it would lean out and backfire after it warmed up and eventually would not restart when warm.
Fix: New coil and module. GM HEI was only a few years old, but as we know that doesn't matter. Upgraded to DUI coil and module and have been running great since.
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1967 C20, 350 SBC w/Comp roller cam, 700R4 w/3.42 posi, PS, 4-wheel PDB, Old Air AC & GM Tilt column. |
08-12-2022, 04:59 PM | #8 |
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Join Date: Apr 2022
Location: Moorpark, CA
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
If the 6 cyl is like the V8, you use a long screwdriver after pulling the dizzy back out and turn the oil pump slightly. Looks like you want to turn it slightly to the right.
Sometimes when you pull the dizzy it turns the pump some so putting it back in same orientation the slot end of dizzy won't engage the pump unless it goes where the pump now is. |
08-12-2022, 05:27 PM | #9 |
Who Changed This?
Join Date: Jan 2013
Location: Simi Valley, CA
Posts: 10,577
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Re: 1968 GMC 250 Inline 6 4.1L Chugging
Looks like you are one tooth off. Do you have before and after pictures of the crank pulley and timing marks?
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~Steven '70 Chevy 3/4T Longhorn CST 402/400/3.56 Custom Camper Simi Valley, CA |
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1968, 250, backfire, chugging, gmc |
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