The 1947 - Present Chevrolet & GMC Truck Message Board Network







Register or Log In To remove these advertisements.

Go Back   The 1947 - Present Chevrolet & GMC Truck Message Board Network > 47 - Current classic GM Trucks > The 1967 - 1972 Chevy/GMC Suburbans & Panels Message Board > 1967 - 1972 Chevy/GMC Suburbans and PanelsProjects and Builds

Web 67-72chevytrucks.com


Reply
 
Thread Tools Display Modes
Old 01-11-2023, 08:39 AM   #926
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

I have one on my 02 sierra because I think it has a battery drain somewhere. but I would feel like it wouldn't idle right when I would disconnect it daily. now it idles fine with the disconnect but now the damn thing dies every now and then lol


problems...
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-11-2023, 04:09 PM   #927
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by HO455 View Post
Judging from the gauge being around the "C" mark and then reading just below HOT when the truck isn't running hot I would say there is an issue with the guage.
When you said you used a stock sender was it a stock sender for the truck as opposed to stock for the engine. The guage requires a specific sender to be accurate.

These threads may help you.

http://67-72chevytrucks.com/vboard/s...d.php?t=587190

http://67-72chevytrucks.com/vboard/s...d.php?t=726700
followed one of them links and they posted a temp sender part number. i tried that one and it seems i had the wrong one (rock auto ) warmed it up today and this is where the needled sat, with a cheap thermo gun pointed at the pump it read about 190 ish

thank you!
Attached Images
 
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-14-2023, 12:17 PM   #928
HO455
Post Whore
 
HO455's Avatar
 
Join Date: Feb 2016
Location: Portland Oregon
Posts: 11,301
Re: Project 67 DRGNWGN - 67 Burban!!

You're welcome! Glad to see more progress.
__________________
Thanks to Bob and Jeanie and everyone else at Superior Performance for all their great help.
RIP Bob Parks.
1967 Burban (the WMB),1988 S10 Blazer (the Stink10 II),1969 GTO (the Goat), 1970 Javelin, 1952 F2 Ford OHC six 4X4, 29 Model A, 72 Firebird (the DBP Bird). 85 Alfa Romeo
If it breaks I didn't want it in the first place
The WMB repair thread http://67-72chevytrucks.com/vboard/s...d.php?t=698377
HO455 is offline   Reply With Quote
Old 01-18-2023, 07:45 PM   #929
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

well, finally got some stuff buttoned up. had to redo the passenger side exhaust. finished up the e brake install, that was interesting with the exhaust all up in the way. i moved it for the first time in like 8 or 9 years i think it was. got some bugs though before i try to move it around the block. brake pedal SLOWLY comes back up after pressing it..need that figured out. the start up on it has been very odd, but after numerous crank and runs it finally stayed on and ran normal. i will try again tomorrow to see how it cranks and stays on.

im super excited because i think FINALLY i might be able to make the local car show this year in june....well see though.
Attached Images
 
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-18-2023, 07:55 PM   #930
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

I did want to describe the engine running problem, maybe it's normal? so.. I never had any issues with the trucking turning on and running before I did the exhaust.

truck starts.. after a few cranks... runs a little rough, sputters for a few seconds dies. it did this over and over.. maybe and 10-12 times. periodically I would press the pedal and rev it it some. some times it would stay running, sometimes the pedal pressing would kill it. unplugged MAF, plugged in, no change either way... still dies.

I got frustrated, disconnected ground on the battery, pulled intake and MAF. cleaned MAF with cleaner, cleaned throttle body a little with cleaner. installed everything back and same results. on about the 3rd crank after this, I constantly kept reving the truck with the pedal, about 2000 rpm, up and down. finally it stayed running and idled great.
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-18-2023, 10:02 PM   #931
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post
I did want to describe the engine running problem, maybe it's normal? so.. I never had any issues with the trucking turning on and running before I did the exhaust.

truck starts.. after a few cranks... runs a little rough, sputters for a few seconds dies. it did this over and over.. maybe and 10-12 times. periodically I would press the pedal and rev it it some. some times it would stay running, sometimes the pedal pressing would kill it. unplugged MAF, plugged in, no change either way... still dies.

I got frustrated, disconnected ground on the battery, pulled intake and MAF. cleaned MAF with cleaner, cleaned throttle body a little with cleaner. installed everything back and same results. on about the 3rd crank after this, I constantly kept reving the truck with the pedal, about 2000 rpm, up and down. finally it stayed running and idled great.
I wonder if it could be a bad 02 sensor or maybe carboned up a little, or connector not plugged in all the way? Hopefully after you run it a little more it will straighten itself out.....

On the brake issue, it sounds like your return spring is either broken or missing. One end of it fastens in a bracket right by the brake light switch and the other end fastens up by the firewall. It will be white or blue in color. Don't pay any attention to the labels.

LockDoc
Attached Images
 
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-

Last edited by LockDoc; 01-18-2023 at 10:14 PM.
LockDoc is offline   Reply With Quote
Old 01-18-2023, 10:36 PM   #932
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

hey Leon... I bought new o2 sensors last week and put them in, same issue... I'll check the plugs. I cranked it again about an hour after shut down and it started right up.

I checked the spring last week and it's there for sure.... wonder if it could be worn out. is it a common issue?
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-19-2023, 02:40 PM   #933
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post
hey Leon... I bought new o2 sensors last week and put them in, same issue... I'll check the plugs. I cranked it again about an hour after shut down and it started right up.

I checked the spring last week and it's there for sure.... wonder if it could be worn out. is it a common issue?

Good deal on the startup. That is a good sign.....

I don't think you are going to ever wear that spring out. It is tough. I have seen them break though, that is why I asked.

I found this post by Accelo:

Quote:
Your Pedal check valves are damaged. Power brake sluggish return is almost always the relief valve built into the sealing ring at the plunger input failing to let in fresh air and you're fighting a vacuum from the other side. It allows the diaphragm spring to overcome the engine vacuum and return the brake pedal to the normal position. In all likelihood you will need to replace or rebuild the booster.
Another thing you can try is to unhook the vacuum line to the booster (plug the manifold side) and see what the pedal does.

LockDoc
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-

Last edited by LockDoc; 01-19-2023 at 02:46 PM.
LockDoc is offline   Reply With Quote
Old 01-19-2023, 11:39 PM   #934
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

ran it for a bit today and it finally showed a code. p0102, which is low voltage from the MAF. going to try and see what I can read on that one, other than just buying a new one and hope it fixes it.

I went back and forth in the yard a little stopping and going and noticed the pedal was a little erratic. it press real easy sometimes, sometimes it wouldn't. if I pumped them a lot it would return like normal, and sometimes not.... and of course the slow return was still there. I tried adjusting the rod nut on the pedal but no change.

the booster is new... but from about 8-10 years ago. it sat for a while and rusted up. when I pulled it off last year I just repainted it and bought another master cylinder. so who knows, maybe the booster is leaking on the inside


I did unhook the vac hose on the booster while it was running and started stumbling and wanted to turn off... so I just hooked it back up
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]

Last edited by kev2809; 01-19-2023 at 11:57 PM.
kev2809 is offline   Reply With Quote
Old 01-20-2023, 12:13 AM   #935
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post

I did unhook the vac hose on the booster while it was running and started stumbling and wanted to turn off... so I just hooked it back up

That is why I mentioned in my post above to plug the manifold side of the line...

LockDoc
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-
LockDoc is offline   Reply With Quote
Old 01-20-2023, 07:39 AM   #936
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

oops haha I'll see if I have something to plug it. what "should" the pedal do with no vaccume? return like it should?

I was thinking of buying those cheapo harbor freight vaccume testers and see if I could test the booster on the truck
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-20-2023, 11:15 AM   #937
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post
oops haha I'll see if I have something to plug it. what "should" the pedal do with no vaccume? return like it should?

I was thinking of buying those cheapo harbor freight vaccume testers and see if I could test the booster on the truck

Not sure if it will make a difference or not. I guess you could just press the brake pedal without the engine running and see how it returns. That should produce the same results because there would be no vacuum.....

Do you remember if the pedal moved freely before you bolted up the pedal to booster bellcrank rod?

LockDoc
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-
LockDoc is offline   Reply With Quote
Old 01-20-2023, 12:49 PM   #938
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

well with the truck off i can press the pedal down (it is stiffer than when the truck is on) and it returns normal. it only does it when its running, i bench bled the master cylinder, then i bled the truck twice. i mean, i guess it could still be air but idk.

i popped the hood today and noticed theres a leak between the master and booster. the master i bought here off the board brand new, believe it was old stock. im thinking maybe a new booster and master is something i might be buying......again

im wondering if ONLY the master cylinder leaking could be causing the slow pedal return...i just dont want to have to pull the master, replace it, bleed out the system...only to realize the booster was bad too lol
Attached Images
 
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-20-2023, 05:03 PM   #939
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post
well with the truck off i can press the pedal down (it is stiffer than when the truck is on) and it returns normal. it only does it when its running, i bench bled the master cylinder, then i bled the truck twice. i mean, i guess it could still be air but idk.

i popped the hood today and noticed theres a leak between the master and booster. the master i bought here off the board brand new, believe it was old stock. im thinking maybe a new booster and master is something i might be buying......again

im wondering if ONLY the master cylinder leaking could be causing the slow pedal return...i just dont want to have to pull the master, replace it, bleed out the system...only to realize the booster was bad too lol

I don't think the master cylinder could cause that, and I don't think it's air in the system. I guess I would be leaning towards the booster. Do you have an old booster you can try? You can change the booster without disconnecting the brake lines. Just unbolt the master and pull it forward enough to unbolt and remove the booster.....

LockDoc
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-
LockDoc is offline   Reply With Quote
Old 01-20-2023, 05:16 PM   #940
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

i dont have an extra one. i dont mind buying a new one if thats what it is, but the leak in between the master cylinder and booster would also mean that the master cylinder would be bad, right? what im thinking is two seperate problems..the booster maybe damaged on the inside causing the poor pedal return, but master cylinder is also leaking where the booster push rod goes in..
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-20-2023, 05:28 PM   #941
3757chevy
Senior Member

 
3757chevy's Avatar
 
Join Date: Mar 2016
Location: Near Canon City ,Colorado
Posts: 4,033
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post
i dont have an extra one. i dont mind buying a new one if thats what it is, but the leak in between the master cylinder and booster would also mean that the master cylinder would be bad, right? what im thinking is two seperate problems..the booster maybe damaged on the inside causing the poor pedal return, but master cylinder is also leaking where the booster push rod goes in..
I agree. Leak into the booster from master may not be all the problem . The booster sitting unused for time might cause issues in my opinion.
__________________
'35 1/2 ton Pickup (bought 2020) '68 C10 Suburban (bought 2021) '72 K5 Blazer (bought 2013)
'67 Stepside (bought 1997-sold 2021) '96 Bronco Eddie Bauer (inherited 2010)
My 1st day here-'67 C10(sold)and '72 K5 Blazer http://67-72chevytrucks.com/vboard/s...d.php?t=702056
MIKE
3757chevy is offline   Reply With Quote
Old 01-20-2023, 05:42 PM   #942
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

ya..and it was rusted up good. i hit it with a wire wheel and cleaned it up before painting it...but it probably sat in the truck unused nearly 10 years. im looking around now to see if i can find booster/master cylinder combo thats reasonable. stuff went way up since i bought these the first time..as has everything else
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-21-2023, 06:39 PM   #943
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

went ahead and ordered a whole new booster/master cylinder/prop valve setup. says its specifically for a 67-72 c10 with front disc rear drums. hopefully that solves the brake pedal issue im having, it will solve the leaking master cylinder for sure at least lol

https://www.ebay.com/itm/1967-1972-C..._redirect=true
Attached Images
 
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-22-2023, 01:26 AM   #944
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post
went ahead and ordered a whole new booster/master cylinder/prop valve setup. says its specifically for a 67-72 c10 with front disc rear drums. hopefully that solves the brake pedal issue im having, it will solve the leaking master cylinder for sure at least lol

I would think that would take care of it. let us know.

LockDoc
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-
LockDoc is offline   Reply With Quote
Old 01-22-2023, 05:00 PM   #945
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

well had a little time to play with the truck while I wait for the booster setup. I took my multi meter and checked the MAF for 12 volt and ground with key and both checked out. my multimeter don't have hertz, so I couldn't check that. but if it's getting power and ground, I figured the MAF may be failing. I replaced with a new one and have the same problem. cranks the second time and idles fine, but bogs under acceleration, and even a little backfire it seems when I rev it in park.

so I rented a fuel pressure tester from. O'Reilly's. I found some off readings. I'll post the picture below, but with key on, and with the engine running... the psi didn't change and showed really low. I tried this gauge on my 2002 avalanche 5.3, and it showed 55, so I know the gauge is working

opinions? I have some time to kill until I get the booster in so I figured I would try and narrow down this stumbling issue.
Attached Images
 
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]

Last edited by kev2809; 01-22-2023 at 05:18 PM.
kev2809 is offline   Reply With Quote
Old 01-22-2023, 05:09 PM   #946
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

I'm running an ACDELCO# EP381 fuel pump, which is listed for a 96-97 Tahoe. that pump should put out enough pressure for the LS motors.

the filter is just a basic stock 2002 Tahoe filter from O'Reilly's.
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-22-2023, 05:39 PM   #947
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

-
I'm no fuel supply guru but I'm surprised it is running at all with that low of fuel pressure. I think it should be 55-60# pressure. I think I would go over to the LSx Swaps forum and ask over there.

LockDoc
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-
LockDoc is offline   Reply With Quote
Old 01-22-2023, 06:40 PM   #948
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

ya I'm surprised too Leon. at first I thought the gauge wasn't right. but when I connected to my other truck I quickly realized it was working.
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-23-2023, 11:36 AM   #949
kev2809
low n' slo
 
kev2809's Avatar
 
Join Date: Mar 2009
Location: rosenberg, texas
Posts: 5,173
Re: Project 67 DRGNWGN - 67 Burban!!

well I MIGHT have found the problem. pulled the fuel pump and the pickup hose wasn't all the way on! straightened it up and dropped it back in and now I'm getting 45 psi running. 55 truck off key on. pressure still seems a little low, pump is listed for a 97 Tahoe which is the TBI motor, but I read this pump is commonly used for LS swaps.

but anyways, I put it in gear and punched it back and forth in the driveway trying to recreate the bog down.. and it didn't do it... ran good it seems. still want to wait til my booster comes in before I can take a spin around the block
Attached Images
  
__________________
67 1/2 ton Suburban - Project DRGNWGN. Build thread

-_--_--_ _________
_--_-_ -/____|__|__\__
,.,,,.,.,,.,|_O _______ O_]
kev2809 is offline   Reply With Quote
Old 01-23-2023, 04:22 PM   #950
LockDoc
The Older Generation


 
LockDoc's Avatar
 
Join Date: Aug 2006
Location: Montezuma, Iowa
Posts: 25,659
Re: Project 67 DRGNWGN - 67 Burban!!

Quote:
Originally Posted by kev2809 View Post
well I MIGHT have found the problem. pulled the fuel pump and the pickup hose wasn't all the way on! straightened it up and dropped it back in and now I'm getting 45 psi running. 55 truck off key on. pressure still seems a little low, pump is listed for a 97 Tahoe which is the TBI motor, but I read this pump is commonly used for LS swaps.

but anyways, I put it in gear and punched it back and forth in the driveway trying to recreate the bog down.. and it didn't do it... ran good it seems. still want to wait til my booster comes in before I can take a spin around the block


Yes, I think the TBI pumps are a little low on pressure. I don't know what the down side might be....

Does the end of your tube have a bubble on it? If not you may have problems with it again after a while. Lot of pressure for no bubble and 1 clamp. I put 2 of the special fuel injection clamps on mine but it looks like you are a little short on space there.

LockDoc
__________________
Leon

Locksmith, Specializing In Antique Trucks, Automobiles, & Motorcycles

(My Dually Pickup Project Thread)

http://67-72chevytrucks.com/vboard/s...d.php?t=829820

-
LockDoc is offline   Reply With Quote
Reply

Bookmarks


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -4. The time now is 12:30 AM.


Powered by vBulletin® Version 3.8.11
Copyright ©2000 - 2024, vBulletin Solutions Inc.
Copyright 1997-2022 67-72chevytrucks.com