05-13-2024, 02:22 PM | #951 |
laying low
Join Date: Mar 2001
Location: Searcy, Ark. USA
Posts: 13,461
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Re: What did you do to your truck today??
Ttt
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Boog 69 Chevy stepside, 358/T350, 4.11 posi, 4.5/4 drop, rallys, poboy driver primer is finer 91 Chevy sportside, Tahoe, Yukon & GMC Crewcab All GM..'nuff said. I stand for the flag and kneel at the cross |
05-20-2024, 02:37 AM | #952 |
Senior Member
Join Date: Jan 2005
Location: CA
Posts: 5,836
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Re: What did you do to your truck today??
Noticed the pinion seal was leaking on my 89 K1500, so I replaced it today.
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05-20-2024, 10:54 PM | #953 |
All about them K’s
Join Date: Jun 2014
Location: Land of Entrapment
Posts: 6,454
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Re: What did you do to your truck today??
I swapped out the 16x10” Mickey Thompson classic 2’s with circa 2010 Baja atz’s, for a new set of moto metal 20x10’s with 35x12.5 Toyo MT’s on Saturday. Also changed the valve cover gaskets, oil in both diffs and the engine oil and filter. Shes getting ready to go back to daily duty next week after sitting the better part of 9 years on and off.
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Tyler '57 3100 http://67-72chevytrucks.com/vboard/s...d.php?t=813888 '72 K20 Cheyenne: 5” lift, 35’s, front dana 60 blah blah blah… http://67-72chevytrucks.com/vboard/s...d.php?t=662879 ‘69 K10 SWB: 4” lift 33”s… in a million pieces http://67-72chevytrucks.com/vboard/s...d.php?t=805206 '98 Silverado LT K2500HD ECLB Vortec 454/4l80E: 6" lift 35x12.5x20’s |
05-31-2024, 03:39 AM | #954 |
Senior Member
Join Date: Jan 2005
Location: CA
Posts: 5,836
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Re: What did you do to your truck today??
My '89 K1500 has had a minor transmission fluid leak from the front of the transmission since I bought it about two years ago. The torque converter clutch started shuddering recently, so I dropped the transmission, replaced the pump seal and replaced the torque converter. It's back together. The TCC is locking solidly once again, and the dust shield is staying dry.
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09-14-2024, 10:01 PM | #955 |
Senior Member
Join Date: Jan 2005
Location: CA
Posts: 5,836
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Re: What did you do to your truck today??
My previous attempt to fix a leak on the front pump of my transmission failed. I pulled the transmission and rebuilt it over the course of this past week. Found a couple broken parts inside. I believe this is the first time this transmission has been rebuilt. It has 300,000 miles on it. Reinstalled it today and took it for a 60-mile drive with no issues.
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09-15-2024, 08:14 AM | #956 |
laying low
Join Date: Mar 2001
Location: Searcy, Ark. USA
Posts: 13,461
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Re: What did you do to your truck today??
Got your money's worth out of that one.
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Boog 69 Chevy stepside, 358/T350, 4.11 posi, 4.5/4 drop, rallys, poboy driver primer is finer 91 Chevy sportside, Tahoe, Yukon & GMC Crewcab All GM..'nuff said. I stand for the flag and kneel at the cross |
09-15-2024, 09:53 AM | #957 |
Senior Member
Join Date: Jan 2005
Location: CA
Posts: 5,836
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Re: What did you do to your truck today??
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11-15-2024, 05:29 PM | #958 |
Registered User
Join Date: Oct 2016
Location: Dallas Texas
Posts: 3,166
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Re: What did you do to your truck today??
.
Been hunting down a hard misfire just off idle at throttle tip in either from a stop or cruising real slow. One day it happened, sounded like the thing was running on every other cylinder for just a second or so then back to normal. Since I had been adjusting and tuning the EFI parameters and hardware blade settings, I figured it was just a fuel map issue fouling plugs...something that it would "learn" to do right with time. This kept happening...usually after a little heat soak and the frequency increased. I tested things by swapping out the throttle body EFI --I have a spare-- with all its internal sensors and the main power module for the EFI --I have a spare--. No change. The ignition box and the coil tested out good with no faults and cap/rotor has wear but not damaged. Timing was where it should be (mechanical timing). I could reproduce the missfire(s) easily enough and while doing so had a number of back fires out exhaust and popping out of the throttle body. So decided it's not fuel/air so must be spark. Swapped out the coil with a new one and POOF! problem solved. The multimeter on the bench with new and old coil showed the old one had more resistance across either + or - and the <output> terminal but no dead shorts or open circuits. Fun...fun. -Kevin
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67 C10 fleet fuel injected '70 402, 700r4, 3.73 posi 07 335 sport turbo 6sp 94 Trans Am GT LT1 6sp posi -- sold after 22yrs 99 540 sport V8 6sp -- sold 73 240z L24 4sp -- given to friend 68 C10 step 350/350 3.73 open -- sold Last edited by weq92f; 11-16-2024 at 07:22 PM. |
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