12-09-2018, 11:12 PM | #126 |
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Re: What did you do to your truck today.The 3rd chapter
Went to summit to pickup a new GM 350 crate engine. My old engine has numerous issues and now it is using oil.
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68' with no bells or whistles unless I add'em. |
12-10-2018, 08:38 PM | #127 |
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Location: eastern Washington
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Re: What did you do to your truck today.The 3rd chapter
Out with the old seat, in with the new (to me) seat, plus a new dash pad, refurbished cluster bezel, and door handle and window crank escutcheons. I'm going to install the new glove box liner as soon as I get my radio fixed and installed.
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12-12-2018, 05:55 PM | #128 |
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Re: What did you do to your truck today.The 3rd chapter
Readied my new engine for installation.
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68' with no bells or whistles unless I add'em. |
12-13-2018, 05:04 PM | #129 |
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Re: What did you do to your truck today.The 3rd chapter
https://photos.app.goo.gl/f7YgUPK1Kv9zrdr77
This wasn't today, it was Monday, but I finally got my grandad's truck moved to my house. But not after it was broken into, and a bunch of new parts stolen. But she's safe in my driveway now. I still haven't gotten this adding photos down, it wasn't showing up, so i just added a link to the photo |
12-13-2018, 05:18 PM | #130 |
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Re: What did you do to your truck today.The 3rd chapter
Here yah go OldBlue70C10
Last edited by nlped; 12-13-2018 at 05:25 PM. |
12-13-2018, 05:20 PM | #131 |
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Re: What did you do to your truck today.The 3rd chapter
Thanks! I appreciate that
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12-16-2018, 08:16 PM | #132 |
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Re: What did you do to your truck today.The 3rd chapter
Got a little closer to starting it!
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68' with no bells or whistles unless I add'em. |
12-16-2018, 09:19 PM | #133 |
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Re: What did you do to your truck today.The 3rd chapter
Finished redoing the AC box under the hood. The goal was functionality, and to stop being a hostel for furry rodents. Originally, the inboard side of the box had two holes where the original vacuum canister had been mounted. Sometime in the past 50 years, it was forcibly removed, leaving two perfect mouse sized holes. So, took it upon myself to try and repair it by doing fiberglass for the first time ever. Of course, after removing the whole system and getting rid of the old mouse funk...
Before, during, and after: This is an AC truck, but the system had been open to the elements for who knows how long, so instead of reinstalling the non-working evaporator, rusty POA and other stuff, I simply plugged the two grommets to try and seal up the case. Also, fiberglassed a metal bar to the inside of the side panel with tapped threads I can remount the replacement vacuum canister.
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1970 C10 CST, PS, PB, AC, patina, original, work in progress |
12-16-2018, 09:29 PM | #134 |
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Re: What did you do to your truck today.The 3rd chapter
After the AC box was back in, I decided to take a look at the drip rail to see how difficult it would be to remove. Tried to pry a little of the old, dried, separated seam sealer, and before I knew it, I had most of it out. And, I had told my wife that I was going to wait on that job.
Most of it came out fairly easily, then I attacked it with a wire wheel. Some surface rust, but no holes and no rust through!! So, decided to use some rust reformer just to make sure there wasn't something hidden, so masked it all up and shot a coat on it. The goal is to let this cure overnight, then tomorrow evening I am planning to attempt to redo the seam sealer. I have the 3M 8307 for the horizontal section, then 8308 for the vertical sections. Never done seam sealer before, so it should be interesting...
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1970 C10 CST, PS, PB, AC, patina, original, work in progress |
12-16-2018, 09:53 PM | #135 |
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Re: What did you do to your truck today.The 3rd chapter
I finally got the spot light in. That drilling is a nerve wracker! But it's done and tested. Final wiring will be done sometime this week we ran out of day light.
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1971 LWB Custom, 6.0LS & 4L80E, Speedhut.com GPS speedometer & gauges with A/C. 20" Boss 338's Grey wheels 4 wheel disc brakes. My Driver Seeing the USA in a 71 Upstate SC GM Truck Club 2013,14 and 2016 Hot Rod Pour Tour http://upstategmtrucks.com/ Get out and drive the truck this summer and have some fun! It sucks not being able to hear! LWB trucks rule, if you don't think so measure your SWB! After talking to tech support at Air Lift I have found out that the kit I need is 60811. Per the measurements I gave them. Ride height of truck inside spring and inside diameter of springs. |
12-16-2018, 10:15 PM | #136 |
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Re: What did you do to your truck today.The 3rd chapter
All new ball joints and steering arm linkage and an alignment. Drives way better now.
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12-16-2018, 11:39 PM | #137 |
At the body shop.
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Location: Land of fruits and nuts.
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Re: What did you do to your truck today.The 3rd chapter
Dimmer switch died on the way home.
Transmission mount needed some attention and some quality time spent.
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12-18-2018, 04:21 PM | #138 |
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Re: What did you do to your truck today.The 3rd chapter
Received my replacement heater control levers from LMC Today . I got mine replaced in my '67, I ordered one for my Daughters defrost lever for her '72 and and extra air/fan lever , just because.
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'35 1/2 ton Pickup (bought 2020) '68 C10 Suburban (bought 2021) '72 K5 Blazer (bought 2013) '67 Stepside (bought 1997-sold 2021) '96 Bronco Eddie Bauer (inherited 2010) My 1st day here-'67 C10(sold)and '72 K5 Blazer http://67-72chevytrucks.com/vboard/s...d.php?t=702056 "Another Blue Chevy"(1935) http://67-72chevytrucks.com/vboard/s...d.php?t=799203 MIKE
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12-18-2018, 06:02 PM | #139 |
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Re: What did you do to your truck today.The 3rd chapter
Fitted new door handles, new hood emblem.
Also got to put registration plates on her. That felt good, 3 months of it sitting in the driveway, now I can drive it. |
12-18-2018, 11:37 PM | #140 |
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Location: Simi Valley, CA
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Re: What did you do to your truck today.The 3rd chapter
Discovered that the kluge fitting setup on one of the aftermarket trans cooler lines is leaking. It goes from 5/16" tube to 1/8" pipe to some other fitting to some other fitting to 3/8" hose. I am looking for a fitting that adapts from 5/16 compression to 3/8 hose in one step. I'm convinced that it exists, I just have to go look for it. Tomorrow morning is soon enough.
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~Steven '70 Chevy 3/4T Longhorn CST 402/400/3.56 Custom Camper Simi Valley, CA |
12-22-2018, 04:25 PM | #141 |
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Re: What did you do to your truck today.The 3rd chapter
I installed a new heater box resistor and blower switch. I've got all three speeds now, was missing the high setting, and installed a new glove box. Didn't have as much luck with the glove box light assembly. The thing fell apart when I tried to put it in. Some of these parts are pretty clunky junky!
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Phil "Money is only a tool to create and achieve what you want most in life" PayPal: rodnrudy@comcast.net |
12-23-2018, 01:04 PM | #142 |
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Re: What did you do to your truck today.The 3rd chapter
Original glove box came with a light?
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72 White Cheyenne, The Ghost |
12-23-2018, 01:18 PM | #143 |
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Re: What did you do to your truck today.The 3rd chapter
.
I would think if so, it would have been later, like 71/72. LMC lists the part through the entire range though... -klb
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67 C10 fleet fuel injected '70 402, 700r4, 3.73 posi 07 335 sport turbo 6sp 94 Trans Am GT LT1 6sp posi -- sold after 22yrs 99 540 sport V8 6sp -- sold 73 240z L24 4sp -- given to friend 68 C10 step 350/350 3.73 open -- sold |
12-23-2018, 01:19 PM | #144 |
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Re: What did you do to your truck today.The 3rd chapter
New wheel, smaller than my old one, shorter adapter = a little more leg room
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12-23-2018, 02:04 PM | #145 |
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Re: What did you do to your truck today.The 3rd chapter
In my sideways glove box pic you can see in the upper left hand corner a hole for the switch, the lite would be on the other end. My 68 didn't have a lite and I've not seen one in any truck but I thought it would be neat. Also my wiring harness has the hot wire for the lite. American Autowire harness by the way.
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Phil "Money is only a tool to create and achieve what you want most in life" PayPal: rodnrudy@comcast.net |
12-23-2018, 02:57 PM | #146 |
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Re: What did you do to your truck today.The 3rd chapter
Killed my transfer case. Still drives fine in 2 wheel drive but locks up after about 50 feet in 4.
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Nick 1961 Apache short stepside 4X4 SBW 348/4 speed 1960 Apache C-20 long fleet custom cab BBW 283/4 Speed 1967 rust bucket Olds Cutlass with a 455 1972 GMC K-15 350/4 speed long fleet |
12-23-2018, 06:27 PM | #147 |
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Re: What did you do to your truck today.The 3rd chapter
Well since I love a challenge and I was bored today and pissed about that glove box switch that broke, I decided to see if I could fix it. So I fired up the mig and was able to tack weld the the metal piece back together without melting it. Put it back together, installed it in the glove box, wired it up and Viola I've got a working glove box light! Truck's probably worth a lot more now,LOL
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Phil "Money is only a tool to create and achieve what you want most in life" PayPal: rodnrudy@comcast.net |
12-23-2018, 06:37 PM | #148 |
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Re: What did you do to your truck today.The 3rd chapter
Finished clamping my fuel lines to the frame.
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71 Chevy C10 Shortbed Stepside. LT1 with 4l60E. Just got back from painter, in assembly now. |
12-26-2018, 01:18 PM | #149 |
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Re: What did you do to your truck today.The 3rd chapter
Well this past week i cleaned the cab out including the fuel tank, installed dynamat type product, cut the jute backing for under the carpet and test fit the carpet. still trying to decide if i should put the seats in from a 2013 Silverado i purchasd from LKQ or just the bench seat. problem is i dont have the know how to weld and i need a frame made for the silverado seat as i don't want to drill holes into the cab. The bench seat is perfect i just wanted the silverado seats in it.
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12-26-2018, 02:08 PM | #150 | |
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Re: What did you do to your truck today.The 3rd chapter
Quote:
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