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Old 08-03-2002, 06:58 PM   #1
Blue_71
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just back from Huck's

just got back from the cookout at Huck's, meet oldpaint, high724x4, longhornmail, peirce, of course huck, and jamie, i think his board name is jamie72? i got his real nam ebut not the board name. got the 400SB from andy, andy got his chrome glovebox door, we all got some really good food, and talked trucks out on the back porch. i took some pics of the trucks, and of course andy (cut up ) possed next to the GMC. he said he thought his cam bearings were going though so if hes not on untill late late tonight we know to go looking for him along the interstates. also got pics of some street rods rolling down the interstate, and one of peirce's 37? i think was the year, chevy.
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1971 Chevy Custom/10 (first truck) 350, NV3500 5 speed
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1974 Chevy Custom Deluxe/10
1979 Chevy Custom Deluxe K10 farm truck beater
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Quote:
Originally Posted by Alan Jackson, Cause I'm a country boy
35s whinin on the asphalt, grabbin mud, throwin up some red dirt
R.I.P. Michael Stilts... I will always love and miss you brother! (9-12-80, murdered 4-9-05)
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Old 08-03-2002, 09:48 PM   #2
racedvl
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Sounded like it was a good ole' time.
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Old 08-04-2002, 12:12 AM   #3
LMN8R
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Unhappy

I sure wanted to go, but the lack of funds kept me close to home. I bet it was a really good time. Maybe I'll make it next time, I'd really like to meet some of you guys(and gals).
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Old 08-04-2002, 12:23 AM   #4
Longhorn Man
its all about the +6 inches
 
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I just got back about 20 min ago...(11:30-ish eastern) Trip went awsome. Everything went pretty close to planned for me.
Even though I did get lost and wandered around the backwoods areas...bout 50 - 60 miles added, scared to hell that my cam bearings were going to leave me stranded...almost out of gas, (had 1 gallon left by the time I found a pump) no one could give me good directions, and only one of those little towns had a gas station that i saw. Scared sh!tless. I had to ask 5 ppl how to get there, got 5 differant stories...and no one had a map (not even the gas station????)
So anyways, I finally got there, we all meet, had some awsome eats, .B.S. around, then we look at my truck....
It was makin a very loud metalic grinding/squeeling noise...I was able to hear it over my pipes (or lack thereof) and through the ear plugs, the faster I went, the louder it got. I did the screwdriver to the ear trick, and discovered the water pump, alt, and power steering was all good, no noise. IT was coming from the front of the motor, and my oil psi hasn't been to great lately. Safe asumption. It was also running 200 - 210 instead of 160 - 180.
Then huck discovers the fan clutch is locked up. WTF??? It was only 2 years old!!!!He pulled one out of a scrap pile, and INSTALLS IT for me!!!! Awsome huh?
When the old one hits the grass, we pick it up, and make it turn in the clutch...there's my noise.
Phew.
Well, not only did it go flawless after that, but those torque pluss intake gaskets...AWSOME! I finaly tuned it with MUCh less timing, (10BTDC instead of about 16-18) Not only is the power alot better....the MPG went up from 9 - 10 up to 13 - 14 at a higher rate of speed. I averaged 80 all the way home and got 14.
Awsome huh?
Huck, thanks for the get together, glad to meet everyone....I had a blast.

Last edited by Longhorn Man; 08-04-2002 at 10:59 AM.
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Old 08-04-2002, 11:10 AM   #5
Longhorn Man
its all about the +6 inches
 
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ttt
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