03-14-2011, 09:19 PM | #1 |
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Location: Louisville ky
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What did i do wrong?
My waterpump on my 83 was leaking so i took everything apart, replaced the pump cleaned new to this truck pump them the block them used rtv to glue the gasket to the pump put everything back together then added water and it poured out of the bolt hole right above bottom rad hose, i replced gasjet again cleaning everything again it still leaked i finally used two gaskets and stopped the leak but now im paranoid it might blow the gasket out
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03-14-2011, 09:23 PM | #2 |
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Location: Canton/Holly Springs Ga
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Re: What did i do wrong?
is the pump warped somehow? how many miles on pump? new ones fairly cheap
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03-14-2011, 09:38 PM | #3 |
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Re: What did i do wrong?
Im dead broke so i pulled the pump off the 305 i had sitting in the corner, its supposed to have around 100,000 but the van ran fine had no leaks trans went out and it sat for 10 yrs before we pulled the motor and scrapped the van, but i checked the suface it loojex flat and clean
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03-15-2011, 12:07 AM | #4 |
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Re: What did i do wrong?
Just to add i had to modify a few things to get it to work because its off of a late70's gmc van and now on an 83 chevy, so a few acessories didnt line up
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03-15-2011, 12:13 AM | #5 |
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Re: What did i do wrong?
You do know that when the water pump goes out, they leak out of that little hole behind the pulley?
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03-15-2011, 02:45 AM | #6 | |
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Re: What did i do wrong?
Quote:
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03-15-2011, 10:12 AM | #7 |
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Re: What did i do wrong?
Darush. If you used RTV to seal the gasket to the pump & block chances are more than good that teh gasket split because the RTV acts like a lube on the gasket. The space between the hole and the outside is pretty small. First check to see if the mounting flanges on the pump are flat and free of defects. Next, when you install the pump, IF you use a sealer, use a contact type cement or shellac based sealer. Lastly, use a thread sealer on the bolts like pipe dope or GM part #1052080 pipe thread sealer. Let us know how you make out. Jim
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1984 K20 350M engine with 465,000 miles. Well, it's finally done!! Almost 2 years of work, but it was really worth the effort. Little stuff left to do is mount winch, wet sand & buff out and build belly pan\running boards. Body work takes lots and LOTS of beer!!!! God, Guts and Guns made America and God, Guts and Guns will preserve it! The worst thing you could do is get into my sights, but that don't matter, you'll never know it, cause you'll never hear the shotJim or Paladin whichever you choose. |
03-15-2011, 10:49 AM | #8 | |
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Re: What did i do wrong?
Quote:
That may be the issue, or the mount of the pump itself might be pitted, or not not be true....
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03-15-2011, 06:15 PM | #9 |
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Location: The Dalles, OR
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Re: What did i do wrong?
Mine blew out after about 200 miles because of that rtv crap. NEver using it again. Try taking it off, clean and dry the surfaces very well, use one gasket and see what happens. YOU don't want to lose it 600 miles from home and over 100 miles from the nearest parts store. Trust me.
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03-15-2011, 07:35 PM | #10 |
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Re: What did i do wrong?
It's been a long time since I've put a WP on a chevy. But here's something to consider. Do any other accessories bolt onto that location? Is it possible you left out a spacer on that lower bolt and the bolt is bottoming out and not actually tightening down the WP?
Just a thought, as i said it's been a long time. By the way I wouldn't use that WP off the old motor. The seal is probably very dried out and the rust on the WP shaft and bearing will probably wack out the pump in short time. |
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