The 1947 - Present Chevrolet & GMC Truck Message Board Network







Register or Log In To remove these advertisements.

Go Back   The 1947 - Present Chevrolet & GMC Truck Message Board Network > 47 - Current classic GM Trucks > The 1967 - 1972 Chevrolet & GMC Pickups Message Board

Web 67-72chevytrucks.com


Reply
 
Thread Tools Display Modes
Old 12-22-2003, 02:53 AM   #1
chevyforever
Some like em' long!
 
Join Date: Nov 2002
Location: Grace, Idaho
Posts: 69
Angry desperate for help!

ok, this is on my 82 chevy, but i figure that there may be someone out there that can help me out. the truck has a brand new 900 amp Optima battery, a new 63 amp alternator (second one actually), and a brand new crankshaft and water pump pulley.
NOW for the problem. since i have bought the truck, it has gone through 5 alternator belts! all belts have gone at night with all accesories on (lights, radio, heater, and sometimes with the wipers on also). what happens, is what seams to be an intermintent problem. yesterday, I drove to my brothers house which is 20 miles from mine, all accesories on and everything ok. go to leave so i let it idle for about ten minutes to warm things up good. kick on the headlights and the first few times i slowed down for a stoplight, lights go dim and volt meter drops to 12 volts. get going again and volt meter takes a few blocks till it jumps up to 14 volts again, then i gotta stop and drop off some video returns.get going again and volt meter drops AGAIN, except this time it takes about a mile for it to get back to normal along with some squealing and burnt belt smell. so, ten miles later i stop at a buddies house to visit for just a minute. went to leave, starts ok, and is all good till i kick on the headlights, then the sqealing begins. and doesnt stop, more belt burning, volt gauge still at 12 volts. get about two miles and no more squealing because of no more belt. well it was colder than he!!, so i kept cruisin home (8 more miles) at night with all accesories on cuz it was freakin cold. got home safe and sound, the optima saved my a$$. started it today and put it in the shop to hopefully finally figure this thing out before i drive it anywhere again. this is really long but all help is appreciated because i have done everything i can possibly think of and checked about a million things. thanks
chevyforever
__________________
1971 chevy c10 lwb- 300 hp 350 crate motor, soon to be more with ported and polished 62cc chamber 461 double humps, TH400, 3.73 posi, used to be my uncle's truck

1972 chevy k10 lwb- 350,4 spd, old and tired, dad bought brand new and is now mine

1968 chevy c20 lwb- 327, 4 spd, was originally a 50th anniversary truck

1990 GMC K1500-just my runaround truck

1982 Chevy K10 shortbed, new motor and new paint, another project in the mix of the others.

IMPORTS SUCK!
chevyforever is offline   Reply With Quote
Old 12-22-2003, 03:13 AM   #2
dinnut
Registered User
 
dinnut's Avatar
 
Join Date: Apr 2003
Location: missouri city, tx
Posts: 4,486
are you sure the alternator is putting out enough amps? belt too tight? belt slipping? i dotn know im guessing...
__________________
70 longbed
496/th400/Ford 9"
dinnut is offline   Reply With Quote
Old 12-22-2003, 04:05 AM   #3
casey
Registered User
 
casey's Avatar
 
Join Date: Jan 2003
Location: Kelowna B.C. Canada
Posts: 2,048
i wonder if you belt pulleys are out of align???
casey is offline   Reply With Quote
Old 12-22-2003, 04:19 AM   #4
1969 GMC
Registered User
 
1969 GMC's Avatar
 
Join Date: Feb 2003
Location: The Rubber City
Posts: 5,498
it didn't overheat?
in my old POS festiva, I could only make it about one mile after the alt belt had snapped, when it started to get "warm" and this was in wintertime, too. i know, apples and oranges...but Im just curious.

is your alt belt fully tightened? after you changed it, did you go back a day or two later and retighten?
__________________
1969 GMC K2500
1996 Honda Accord
2007 Kawasaki KLR 650

Last edited by 1969 GMC; 12-22-2003 at 04:22 AM.
1969 GMC is offline   Reply With Quote
Old 12-22-2003, 04:24 AM   #5
Injected68LS1
Registered User
 
Injected68LS1's Avatar
 
Join Date: Jul 2003
Location: So. Cal.
Posts: 389
I would say that you are trying to get too much from your alternator. I would replace it with a 100 amp unit.

Either that or don't drive with all accessories on.
__________________
1968 Chev SWB with 1998 Corvette LS1
305hp and 320 ftlb to the wheels (stock engine!)
AEM EMS and wideband O2 sensors
Bowtie Overdrive's 700R4, stage 3
Baer 4 wheel discs and 20s
http://iciclelanding.com/aperture?album=2049&view=album
Injected68LS1 is offline   Reply With Quote
Old 12-22-2003, 04:26 AM   #6
Injected68LS1
Registered User
 
Injected68LS1's Avatar
 
Join Date: Jul 2003
Location: So. Cal.
Posts: 389
An easy way to check for misalignment is to use a long straight edge and start taking measurements. That should tell you if everything is square or not. that's the only other thing I can think of.
__________________
1968 Chev SWB with 1998 Corvette LS1
305hp and 320 ftlb to the wheels (stock engine!)
AEM EMS and wideband O2 sensors
Bowtie Overdrive's 700R4, stage 3
Baer 4 wheel discs and 20s
http://iciclelanding.com/aperture?album=2049&view=album
Injected68LS1 is offline   Reply With Quote
Old 12-23-2003, 01:30 AM   #7
chevyforever
Some like em' long!
 
Join Date: Nov 2002
Location: Grace, Idaho
Posts: 69
no, i didnt have any overheating problems because the power steering belt goes over the water pump also (a/c setup) all pulleys are lined up perfect and belts were tightened, ran, and then retightened. BUT, i think i found the problem tonight after work. The "voltage reference" (red) wire going to the regulator inside the alternator is hooked up to the starter on the same stud as the big battery positive wire. well, the nut was almost completely off the stud on the starter and the battery wire was on a bind enough that it would still start good, but the other wire was just barely hangin in there. now, i threw on a spare belt i had and fired it up. everything ok so far. i can idle the truck with radio, lights, and heater on and the volt gauge never drops one bit, also can hear the alternator working (whining).

gonna drive it somemore and hope for the best.

what do you think? could this have been the problem?

chevyforever
__________________
1971 chevy c10 lwb- 300 hp 350 crate motor, soon to be more with ported and polished 62cc chamber 461 double humps, TH400, 3.73 posi, used to be my uncle's truck

1972 chevy k10 lwb- 350,4 spd, old and tired, dad bought brand new and is now mine

1968 chevy c20 lwb- 327, 4 spd, was originally a 50th anniversary truck

1990 GMC K1500-just my runaround truck

1982 Chevy K10 shortbed, new motor and new paint, another project in the mix of the others.

IMPORTS SUCK!
chevyforever is offline   Reply With Quote
Reply

Bookmarks


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -4. The time now is 04:20 PM.


Powered by vBulletin® Version 3.8.11
Copyright ©2000 - 2024, vBulletin Solutions Inc.
Copyright 1997-2022 67-72chevytrucks.com