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04-01-2005, 02:03 PM | #1 |
71 DELUX
Join Date: Sep 2003
Location: Northern CA / Sac
Posts: 1,055
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bonehead move... humility is good
Just so you all know...
Several weeks ago after my HEI install, I was complaining about a noticeable power loss after making the swap. Had some good advice about checking the timing and vacuum advance. Yet it was something much simpler than any of that. In my haste and excitement to get everything all back together and fired up, and some engine clean-up after the install (and also due to lack of driving it for the last few weeks) I neglect to notice that one of my vacuum line plugs had popped off! (OOPS) Last weekend I was asking myself, "What is that darn hissing noise?" Sure enough, just had to put my finger over the "sucking" opening and instant power! Tell me I'm not the only to have ever done something so dumb.
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5/4 drop LWB wood bed - 15x8 front 235/60 - 15x10 rear 295/50 2003 FORD Escape 1998 Honda VTR1000 |
04-01-2005, 02:49 PM | #2 |
Registered User
Join Date: May 2000
Location: Flin Flon, Manitoba, Canada
Posts: 8,853
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it always seem to be the little things eh. My humility came when I had #5 and #7 plug wires backwards. Couldn't firgure out the rough running and back firing
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My name's Tim and I'm a truckaholic My 56 Chevy shop truck build http://67-72chevytrucks.com/vboard/s...d.php?t=562795 |
04-01-2005, 02:55 PM | #3 |
68cst_ss490
Join Date: May 2001
Location: edmonton,canada
Posts: 1,363
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DOH...gotta hate when that happens
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Dean edmonton,canada a winter wonderland 2005 Chevrolet Avalanche LT cold air intake, performance exhaust, Comp cams cam, jba shorty ceramic headers. http://www.cardomain.com/ride/3090973 |
04-01-2005, 03:06 PM | #4 | |
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Join Date: Dec 2004
Location: Arvada Colorado
Posts: 1,321
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Quote:
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Larry 1949 Willys CJ2A, Kubota Turbo Diesel engine, Warn Overdrive, 11 inch brakes, 12volt, Warn M8000 Winch "Little Green" 1970 Rustoleum Roller Red C20 Custom Camper 454 TH400 "Big Red" 1971 K20 6.2 Turbo Diesel 4x4 4spd Ranger Overdrive "Pumpkin Wagon" 2005 VW Beetle Diesel 44+ MPG "Silver Bullet" |
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04-01-2005, 08:10 PM | #5 |
Big Block
Join Date: Mar 2005
Location: Durham, N.C.
Posts: 1,649
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I put a HEI in my 72 4x4 suburban drove it for a couple days, no problems! They one day in 4 lanes of rush hour traffic the engine died, No way it was going to start. Got it towed home and found the coil burned up. Put in new coil and back on the road again. Drove for a couple more days no problems. Drove to the store one evening and it failed to start. Had it towed home again. The coil burned up again. That when a freind asked me if it had the ground clip hook to the coil. I said what ground clip? Very expensive mistake!!! B.B.
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04-01-2005, 08:50 PM | #6 | |
Registered User
Join Date: Oct 2000
Location: St. Johns, Arizona
Posts: 2,660
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Quote:
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my 2¢ - t.i.o.l.i. Bowen 1968 K20 fleet 1969 K10 swb fleet 1972 K10 Suburban 1972 C10 lwb step 1992 K1500 'burb 1995 K2500 'burb 1997 C1500 'burb 1999 K1500 2000 K1500 'burb Why do I own so many Suburbans? |
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04-01-2005, 09:01 PM | #7 |
Got Light Emitting Diode?
Join Date: Apr 2004
Location: Newberg, OR
Posts: 2,485
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one of my friends was looking at a 81 GMC 1/2 ton 2wd P/U for 500 bucks. the lady said it had a 4.3L that was put in 7000 miles ago. i was confused, maybe they had done a V6 swap or something. we get there and it has a new crate motor and right on the valve covers it says 350, that was her STUPIDITY. it ran ruff but i told him to buy it, we would fix it. when we got it home i heard one of those darn hissing noises. the splitter that screws into the intake behind the carb for the vaccum lines was cracked at the bottom. so we got a new on and she ran fine. then i did a carb swap on it, the fuel line ruptured and this is what she looked like. thats my humility, good thing it wasnt my truck
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1968 1/2 ton 2wd lwb 6 lug disc and bags up front. Next c notch and rear bags '02 Chevy Silverado LT ext cab short bed 2WD 5/7 drop on 22's(the family car) 1993 Cherokee work ride/weekend wheeler |
04-01-2005, 09:02 PM | #8 |
Account Suspended
Join Date: Feb 2005
Location: Yoncalla Oregon
Posts: 775
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I bought a Ford Focus for my wife to drive...Nuff Said.
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04-01-2005, 09:05 PM | #9 |
Designated A-hole!
Join Date: Mar 2003
Location: South Mississippi
Posts: 36,448
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I bought a Dodge Intrepid for my wife to drive......she insisted tho.
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"If it ain't broke, fix it 'til it is!" Being stupid ain't illegal. We're Still Debt Free Except for the House!!! www.daveramsey.com 70 GMC SWB Stepside project "Green Booger" soon to be 6.0l/4l80e 93 S-10 "Poppaw's Truck" |
04-01-2005, 09:14 PM | #10 | |
Account Suspended
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Location: Yoncalla Oregon
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04-01-2005, 09:21 PM | #11 |
Senior Member
Join Date: Aug 2004
Location: Kelso,Wa
Posts: 3,637
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My personal favorite bone headed stupid move. I am a truck driver, we had a cummins fuel pump rebuilt on one of our trucks, well I picked it up from the shop & it would not come back down to an idle, making gear shifting next to impossible. Well putting my mouth in gear long before my brain, I went back to the shop & asked them if this was the 1st pump they ever rebuilt, on & on digging the hole deeper. The shop foreman went over to the truck & looked under the throttle & picked out a little rock. Man did I feel stupid!
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04-01-2005, 10:07 PM | #12 | |
Franko72
Join Date: May 2004
Location: Cincinnati,Ohio
Posts: 471
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Quote:
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1972 C20 cheyenne Super 402 BB/400 turbo LWB A/C Tilt, Cruise Control, Saddle tanks, Tach My Home Page Better to burn out than it is to rust |
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04-01-2005, 10:35 PM | #13 |
Where's my beer?
Join Date: Oct 2004
Location: Glen Allen, VA
Posts: 1,772
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Changed the cap a rotor on my 71 Cutlass years ago, and when I was done it wouldn't start for anything. After about 5 minutes of trying, I looked on the radiator support and said, HMMM, why are 2 rotors laying on top? DOH! Of course it fired right up after I actually installed it.
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70 C10, shortstep, .30 over 250,Hurst shifted 3 spd parts hauler. Holley 390, Clifford Intake, Header, ported cylinder head, unknown bigger cam. 79 Corvette L82, 4 spd, black, red interior, headers, flowmasters, and unkown bigger cam. '03 Grand Cherokee Laredo, 4.0 4x4 daily driver. 165K miles, and runs great '08 Tahoe LTZ 4x4 155K |
04-01-2005, 10:41 PM | #14 | |
Account Suspended
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Location: Virginia Beach, Va. U.S.A.
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04-01-2005, 11:13 PM | #15 | |
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Location: ** THE FALL GUY **CHICAGO IL
Posts: 5,883
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i have seen them missing as well......and might even...oooo..have had a few burned coils....DOHOOOOO.... |
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04-01-2005, 11:49 PM | #16 |
Registered User
Join Date: Jul 2000
Location: Victoria,BC, Canada
Posts: 1,300
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20 years ago wheel bearing burnt up, replaced wheel bearing, tightened washer nut as hard as I could, drove 100 yards, replaced wheel bearing again. Read manual.
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71 GMC 1500 LWB |
04-01-2005, 11:55 PM | #17 |
Got Light Emitting Diode?
Join Date: Apr 2004
Location: Newberg, OR
Posts: 2,485
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hahaha
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1968 1/2 ton 2wd lwb 6 lug disc and bags up front. Next c notch and rear bags '02 Chevy Silverado LT ext cab short bed 2WD 5/7 drop on 22's(the family car) 1993 Cherokee work ride/weekend wheeler |
04-01-2005, 11:57 PM | #18 | |
Registered User
Join Date: Mar 2004
Location: Hoytsville, Utah
Posts: 3,365
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I'm just now working through my bone-head move. Last week I got my Panel back together and running, but no oil pressure. Well, very little. Not near enough for the motor to last long. I dug the old bearings out of the trash and miked them, and found them to be .010 over. No markings on them, so I figured they were standard and never checked things when I had it apart. So now I've spent a hundred bucks and three nights and I'm ready for it to go back in. Tommorow I should have oil pressure.
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'68 Panel Project Boogie Chillin' '68 C-10 Ol' Green |
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04-02-2005, 12:29 AM | #19 |
Registered User
Join Date: Feb 2003
Location: Staunton, Virginia
Posts: 554
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Yeh, Iv'e had my share. The last one was this winter. Packed up the wife in the 70 3/4 ton 4x4 and went off to Kwik Trip for a late night cooffee run. Wew get there and shut off the ole girl. Before we go in, I'm messing with the transfer case shifter that I just fixed. We go inside and get coffee, come back out and start her up. I shift to reverse and no go. I shift to drive and no go. After 5 minutes of this and countless F this and F that's. I figure out that I may have put the transfer case into neutral. Sure enough, put it back in 2 high and off we went. Got to love those senior moments.
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04-02-2005, 03:06 AM | #20 |
huh ???
Join Date: Nov 2002
Location: Fredericksburg,Va.
Posts: 3,368
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That's not as bad as my neighbor. He did an oil change on his truck and as he was adding the last quart of oil he remembered he forgot to put the drain plug back in...
Chuck
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90 Blazer Silverado 350w/ 700R4 and 32" Kelly's "I am a bomb technician. If you see me running try to keep up!" |
04-02-2005, 08:50 AM | #21 |
Designated A-hole!
Join Date: Mar 2003
Location: South Mississippi
Posts: 36,448
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At least he remembered before he left the house with no oil in the engine.
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"If it ain't broke, fix it 'til it is!" Being stupid ain't illegal. We're Still Debt Free Except for the House!!! www.daveramsey.com 70 GMC SWB Stepside project "Green Booger" soon to be 6.0l/4l80e 93 S-10 "Poppaw's Truck" |
04-02-2005, 10:03 AM | #22 | |
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Join Date: Oct 2004
Location: Walker Co. Alabama
Posts: 474
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Quote:
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If it don't fit, force it,...If it still don't fit , modify it 'till it does fit !!! Last edited by modifiedGMC; 04-02-2005 at 10:11 AM. |
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04-02-2005, 10:17 AM | #23 |
Senior Member
Join Date: Jun 2001
Location: Shelbyville, KY
Posts: 3,261
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How about plugging the intake manifold where the carb goes with an old sock. then placing a carb on top a few months later---then bolting the carb down and starting it!
Couldn't understand the loss of power till I remembered the sock. That is why when your wife washes socks she often only finds one!!! the truck ran better after a while. Never bothered to go look for the sock ~hehehehe |
04-02-2005, 10:31 AM | #24 | |
Señor Member
Join Date: May 2002
Location: Edge of the world
Posts: 5,367
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04-02-2005, 12:37 PM | #25 |
Unending Project
Join Date: Aug 2003
Location: Sequim, WA
Posts: 337
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One of my best pal's is a body man, and we hesitate to let him work on his own rig. Got over there one day as he was trying to start his truck after installing a new carb.
No start. I looked under the hood and said "Mr. Bill, Where does the fuel line hook up?" Mr. Bill stared at it for ten minutes until I pointed out that the fuel doesn't go into the vacum port. I'll never let him foget it. Piper |
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